Background

In line with the European Union’s goal of achieving climate neutrality by 2050, a significant increase in the use of renewable energy sources is imperative [1]. Drawing from simulations and optimization across 60 comprehensive studies, it is evident that the electricity storage capacity for 100% renewable energy systems is expected to remain below 6% of the total annual energy demand [2]. The strategic redistribution of electricity across various energy sectors can play a pivotal role in reducing the necessary storage capacity and effectively balancing fluctuations in variable renewable energy sources [2, 3]. An alternative approach, power-to-gas (PtG), offers a means of converting electrical energy into chemical bond energy [3]. The biomethane production process involves the transformation of H2 produced from surplus volatile renewable electricity and biogenic or waste CO2 into CH4 through methanogenesis reactions. Biological methanation (BM) serves as both a storage platform for excess renewable power and an eco-friendly means of utilizing CO2 [4]. Furthermore, by enriching biogas containing biogenic CO2, it is possible to generate grid-quality CH4 ranging from higher than 86 to 97% in different countries, particularly in Germany, where it exceeds 96% [5]. This process facilitated via the activity of hydrogen-consuming hydrogenotrophic methanogens in the BM process. This upgraded biogas, characterized by a high CH4 content and low impurities, is known as biomethane and can be readily stored within the gas grid based on countries standards [5], making it a versatile energy source for various sectors [6].

In biological aerobic and anaerobic processes, continuously stirred tank reactors (CSTRs) are standardized. However, when the reactive phases consist of less-soluble gases in aqueous media (e.g., H2) the productivity of the process is restricted by the transferability of gases between the liquid and gas phases [7, 8]. The low solubility of H2 in the aqueous phase can be compensated by increasing the pressure or concentration gradient during the BM process (> 10 MPa) [9,10,11]. Over the past decade, numerous gas–liquid contactors have been proposed at the laboratory, bench, and pilot scales to address the limitations of H2 gas–liquid transfer, and their advantages and disadvantages in the BM process have been extensively reviewed in the literature [4, 12,13,14]. Gas holdup and interfacial area are the underlying factors that influence the selection of reactor types [8]. These key parameters can be enhanced by employing intensive mixing (> 700 rpm) within a submerged reactor (CSTR), which effectively reduces the gas bubble size and prolongs presence in the liquid phase [8, 15]. Nevertheless, the industrial viability of this approach is challenged by factors such as the shear stress imposed on methanogenic archaea, reduction in syntrophic interactions within mixed cultures and parasitic energy drain associated with high rotational speeds, all of which warrant scrutiny [16,17,18].

In contrast to submerged systems, such as CSTRs and bubble columns, where the predominant phase is liquid, fixed-film systems such as packed-tubular reactors and trickle beds have gas as their primary phase [14, 16]. In a system where gaseous substrates predominate, the volume of the solution surrounding the biomass is minimized to provide moisture and nutrients of the biofilm [16]. Therefore, much less energy is required to facilitate the gas–liquid mass transfer.

While tubular reactors (TRs) have not been extensively explored for the BM process, they are well-studied and industrialized for continuous bioprocesses, such as algae production [19, 20]. Extensive discussions in the literature, including their simplicity compared to CSTRs, highlight the advantages of TRs in bioprocesses, offering benefits such as thorough mixing, reduced dead zones and a significantly improved area-to-volume ratio for enhanced mass and heat transfer efficiencies [21,22,23]. In addition, employing helically shaped tubes and generating secondary radial flow can further enhance mixing intensity [24,25,26]. The elongated gas travel path facilitates prolonged interactions between syntrophic microorganisms [27], hydrogenotrophic methanogens and gaseous substrates. Another advantage of TR systems is the absence of back-mixing with the feeding substrates. Despite the potential of TRs, to our knowledge, only a few studies have reported the development of TR in the BM process [16, 26]. Savvas et al. studied a lab-scale packed tubular reactor primarily aimed to reduce the liquid phase [16]. The results demonstrated productivity ranging from 20 to 39 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d} \,\)(liter of methane per liter of the reactor per day) and CH4 purity ranging from 98 to 50% [16]. These findings are noteworthy when compared to other continuous gas–liquid contactors, especially concerning the production of grid-quality biomethane, which typically requires a purity exceeding 90% [13]. Nevertheless, dead phases, clogging, homogeneity of irrigation and biofilm formation are still problems under investigation in such biofilm systems [8]. Hoffstadt et al. introduced a meandering plug flow reactor configuration with an integrated helical static mixer. In this design, microorganisms travel within the liquid phase, while substrates and the product were conveyed in the gaseous phase, mirroring the principles of a bubble column reactor [26]. This approach substantially mitigated the risk of clogging and offered efficient nutrient support in comparison to biofilm reactors, while also being notably more efficient in terms of energy than CSTRs [26]. This study reported a gas fraction of 29%, which was aligned with simulated data. While the study did not provide direct information on the conversion rates, it did mention achieving a commendable conversion rate to the best of our knowledge [26].

In another context, a liquid foam bed photobioreactor was recently developed to enhance the cost-efficiency of algal production by improving the delivery of CO2 and O2 to the liquid phase [28]. A comprehensive screening of surfactants considering foaming quality, non-toxicity, algal partitioning and slow biodegradability led to the selection of the non-ionic polymeric Pluronic® F-68 (PU-F68) for the development photobioreactor [29]. Several other studies have also highlighted the promising application of froth/foam bed gas–liquid contactors, where reactive gas–liquid interfaces can limit the process or microbial growth rate [30,31,32]. The extensive surface area provided by foam-containing systems, relative to other gas–liquid contactors, can facilitate the rate-limiting step of gas–liquid transfer. However, the advantages of surfactant-stabilized foam, such as increased gas holdup and extended gas retention time, may be offset by the accumulation of surfactant at the bubble surface and potentially hindering mass transfer rates owing to the presence of surfactant molecules [33].

The aim of this study is to introduce an enhanced BM system by combining a TR with a stabilized liquid foam bed. The primary objectives were to improve biomethane productivity, maintain biomethane quality for grid injection, and showcase operational flexibility during intermittent cycles. To achieve these goals, a novel laboratory-scale tubular foam-bed reactor (TFBR) was developed by adding PU-F68 to a TR reactor that had been operating continuously at 40 °C for over 3 months. Furthermore, the study evaluated the performance and robustness of the mesophilic TFBR, particularly in response to intermittent H2 feeding after approximately 5 months of continuous operation. Subsequently, the mesophilic TFBR was transitioned to thermophilic conditions at 55 °C to investigate the effect of temperature in the presence of a surfactant on the kinetics of the BM process.

Results and discussion

The BM process spanned a year, using both the TR and TFBR (Fig. 1 and Fig. S.2. Additional file 4). The results from the final stable feeding week of operation are presented below to assess the highest achieved performance of the BM process during these three phases. Furthermore, the robustness of the BM process in such a TFBR system during the partial H2 feeding experiment was exclusively investigated in phase (II).

Fig. 1
figure 1

Schematic overview of the tubular foam-bed bioreactor (TFBR) setup for biomethane production. H2 was produced via a polymer electrolyte membrane (PEM) electrolyser as in the figure. Stabilized bubbles (foam texture) generated by the addition of Pluronic® F-68 (PU-F68) to the nutrient solution. a Foam texture inside the tubing, b and c light microscopic images of stabilized bubbles taken at 100 × and 400 × magnification, respectively

Biological methanation in the mesophilic tubular reactor: phase (I)

The experiment was initiated with phase (I) in the mesophilic TR, involving a continuous 3-month biomethanation of CO2 and H2 (as shown in Table 1). As the biomass grew and adapted to the process conditions, the outlet gas from the TR was consistently monitored and the reactor was fed based on demand (data not shown). The gas profile for the final week of operation indicated an average CH4 concentration of 79.4% [based on the total number of samples taken in the presented phase (n = 80), standard deviation (SD = 3.9%)], where CO2 exhibited variability, averaging 17.0% (n = 80, SD = 4.1%) and H2 showed an average value of 3.6% (n = 80, SD = 4.2%) (Fig. 2a). Excessive CO2 feeding and fluctuations resulted from intentional variations in H2 feeding, aimed at stabilizing the maximum CH4 production while maintaining the H2 concentration below the detection limit of the gas analysis system. As a higher amount of H2 feeding resulted in the presence of unconverted H2 in the headspace, a stoichiometric feeding ratio of CO2 and H2 could not be achieved using TR. The methane production rate (MPR) for the final week was 2.3 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\) (n = 7, SD = 0.5 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)), with \({\text{Y}}_{\text{rel}}{{\text{H}}}_{2}\) of about 68.4% (n = 7, SD = 10.0%) and \( {\text{Y}}_{\text{abs}}{{\text{CO}}}_{2}\) of 43.4% (n = 7, SD = 8.9%) (Fig. 2d). At the end of phase (I), the concentration of suspended biomass dry weight reached approximately 1.5 g/L (The optical density at 600 nm, OD600 = 2.7) [16]. The findings of this study in phase (I) within the TR were comparable in terms of the MPR to other studies using fixed or submerged reactors [6, 13]. However, they still fall short of the reported high-performance continuous systems, such as trickle beds (15.4 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d)}\), packed tubular (27 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)) and cascade reactors (36 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)) [16, 34, 35].

Table 1 Operation regimes for different process phases. Pluronic® F-68 (PU-F68) was added as a surfactant to produce a liquid foam at w/v (%)
Fig. 2
figure 2

Composition of the gas volume fraction and process performance under different operating regimes. Time course of (a) Phase (I): mesophilic tubular bioreactor (TR) at 40 °C; b Phase (II): mesophilic tubular foam-bed bioreactor (TFBR) at 40 °C; c Phase (III): thermophilic TFBR at 55 °C. Box and Whisker plots for \({\text{Y}}_{\text{rel}}{{\text{H}}}_{2}\) (%), \({\text{Y}}_{\text{abs}}{{\text{CO}}}_{2}\) (%) and MPR (\({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)) considering 24 h H2 feeding regime for 7 d in d Phase (I): Mesophilic TR e Phase (II): mesophilic TFBR; f Phase (III): Thermophilic TFBR (short-term disturbance at day 5 not considered in calculations)

In phase (I) of TR, the gas and liquid flow structures were visually characterized as a segmented two-phase flow along the tube length, specifically exhibiting a slug flow pattern (Fig. 3c) [36]. The presence of stable small bubbles within the flow enhances the gas–liquid interaction, fostering increased mass transfer and system productivity. However, owing to the high surface tension of water, bubbles tend to merge upon collision, leading to gas-filled cavities and a reduction in the gas–liquid interfacial area (bubble coalescence). Moreover, the narrow internal diameter of the tube further increases the likelihood of collision and adhesion tendency of the liquid phase [16]. To address this challenge, stabilizing agents such as surfactants can be introduced, absorbing at the gas–liquid interface and promoting bubble stability [37, 38].

Fig. 3
figure 3

Overview of different flow structures in tubular (foam bed) reactor. The flow structure varies based on the liquid fraction and the presence/absence of the surfactant. a Wet foam flow, high-density foam or bubble jamming; b bubbly flow; c slug flow. d H2 bubble gradient in an active biological methanation process reported by Garcia-Robledo et al.; Maegaard et al. (part of figure adapted from Jensen et al. [8, 40, 41])

Biological methanation in the mesophilic tubular foam bed reactor: phase (II)

Complex biological solutions, which include cell debris, proteins, biosurfactants, biopolymers, fatty acids and various essential ingredients for living cells, naturally lead to foam formation when gas is injected through a liquid (i.e., foam formation in bioreactors). Nevertheless, the resilience of the foam and consequently, the efficiency of the gas–liquid mass transfer are intricately affected by numerous factors. These factors include the specific type and concentration of the ingredients, temperature, pressure, flow rheology and degradability of the surfactant [37, 38]. Consequently, PU-F68, a synthetic polymer renowned for its exceptional foaming properties, was strategically selected to establish a stabilized liquid foam within a continuously operating TR [27]. The experiment continued by adding the PU-F68 surfactant to the recirculating liquid phase as a bubble stabilizer and transferring the TR reactor to the TFBR [phase (II) Table 1]. PU-F68 played a pivotal role in reducing the surface tension between the water molecules, thereby enhancing the stability of the micro-bubbles formed after gas injection (Figs. 1a–c and 3a). Beyond the critical micellar concentration (CMC), surfactant molecules aggregate to form micelles, actively contributing to the creation of stabilized bubbles and foam [29]. Following the recommendations of Janoska et al., a concentration of 1.5% (w/v) PU-F68 was deliberately chosen (approximately five times the CMC concentration). This selection aimed to obtain a foam with intermediate stability, roughly translating to a half-life of approximately 1 h [29, 39].

Starting from phase (II), a discernible enhancement in the uniformity of the outlet gas and a notable increase in the MPR were observed. The weekly average concentration of CH4 was recorded at 93.1% (n = 627, SD = 2.1%), with H2 and CO2 concentrations averaging at 2.1% (n = 627, SD = 1.5%) and 4.8% (n = 627, SD = 1.6%), respectively (Fig. 2b). The average weekly MPR experienced an impressive 6.5-fold increase compared to phase (I), reaching a value of 15.1 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d} \,\)(n = 7, SD = 0.4 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)) (Fig. 2e). Achieving a stoichiometric feeding ratio of 4H2: 1CO2 (Fig. 2e), the average relative and absolute conversion yields of H2 and CO2 were calculated at 84.8% (n = 7, SD = 2.1%). In contrast to phase (I) in this study, the performance of the mesophilic TFBR was comparable to that of studies conducted in fixed-film/submerged bioreactors under mesophilic conditions reviewed by other studies [13, 40]. To the best of our knowledge, the highest reported laboratory-scale continuous BM’s MPR value exceeding 90% CH4 concentration was achieved by a cascade packed column reactor (36 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)) running for a limited duration of 37 h due to technical issues [35]. While some studies have reported higher values, they achieved this at the trade-off of methane concentration [6, 13].

The flow structure underwent significant changes following the addition of PU-F68, in contrast to the initial phase (I) within TR and varied along the tube as the BM process progressed. Towards the end of phase (II), where the highly productive BM process took place with a gas-to-liquid feeding ratio of 7:1, the flow can be visually described as follows: at the injection point, the flow predominantly resembled a high-density or wet foam (Figs. 1a, 3a). As the BM process advanced and the gaseous substrates underwent conversion, the bubbles diminished in size and process water was produced. The progression of the BM process along the tube led to an increase in the liquid phase fraction and transition to bubbly flow, where the liquid phase fraction passed the critical bubble jam fraction (Fig. 3b) [37]. Ultimately, at the tube outlet, where the majority of the gaseous substrates were converted, the flow transitioned into slug flow (Fig. 3c). The inherent breakdown of bubbles in the BM process [1CO2 (g) + 4H2 (g) ⟶1CH4 (g) + 2H2O (L)] prevented a further additional step of foam breakage, which was reported in the literature as a subsequent step aimed at releasing the gas phase trapped within the bubbles [41].

Microscale investigations revealed that the BM process was confined to a narrow zone around the gas–liquid surface (< 0.5 mm) (Fig. 3d) [41, 42]. Consequently, the gas liquid mass transfer limitation was identified as a constraining factor for the BM process in the bulk [42, 43]. Despite the variations in bubble size during the BM process, the utilization of PU-F68 to stabilize the small bubbles along the tube markedly enhanced the BM productivity and conversion yields.

The enhancement in gas–liquid mass transfer resulted in a more efficient process and a higher rate of biomass/nutrient recycling. The biomass density was increased to 9.3 g/L (OD600 = 19.6) by the end of the stable running experiment. Although biomass recycling was undertaken under anaerobic conditions to sustain biomass activity, it is acknowledged that this approach may have led to the lysis of certain community members. Existing evidence suggests the advantageous role of biomass lysate recycling in providing essential nutrients during the BM process [27, 35, 44].

Biological methanation in the thermophilic tubular foam bed reactor: phase (III)

The temperature plays a crucial role in gas–liquid reactions, influencing reaction rates, equilibrium constants, and the overall kinetics of the reaction. The effect of temperature can vary depending on the specific reaction and the reaction conditions. In phase (III), the temperature of the mesophilic TFBR system was increased from 40 to 55 °C. At the outset of experiment, biomass concentration decreased by approximately half as a result of temperature shifts; however, after the adaptation phase, it recovered and reached 10.0 g/L (OD600 = 23.5). Towards the end of phase (III), there was a 16-h interruption in the feeding of H2, resulting in a significant increase in CO2 concentration, while the CH4 concentration decreased (Fig. 2c). Upon resuming H2 feeding, the TFBR self-recovered within approximately 8 h, demonstrating capability of the reactor to handle H2 interruption.

Excluding the explained interruption phase, on average, the outlet gas predominantly consisted of CH4 (92.1%, n = 588, SD = 6%), with less than 8% H2 and CO2 (Fig. 2c). The MPR in thermophilic TFBR reached the average value of 29.7 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\) (n = 7, SD = 1.5 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\) compared to 2.3 and 15.1 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\) in phase (I) and phase (II) respectively (Fig. 2d, e). In addition, H2 and CO2 conversion yields reached 96.6% (n = 7, SD = 5%) and 83.4% (n = 7, SD = 4.3%) respectively. Temperature significantly influences the metabolic rate of conversion and the stability of hydrogenotrophic methanogens [6, 45]. Moreover, higher gas–liquid transferability can be achieved at higher kL and lower viscosity, which can be attained at higher temperatures [6]. However, increasing the temperature resulted in a drastic decrease in H2 solubility [46]. Temperature also affects various physiochemical properties of the foam, such as surface tension, CMC, bubble coalescence and stability, underscoring its importance in monitoring the BM process performance and stability [38, 39].

Despite the negative effects of temperature on H2 solubility and foam stability, the thermophilic-enriched community demonstrated an almost twofold increase in the productivity of the BM process compared to phase (II). Studies on microbial community composition and the effect of temperature have suggested that increasing the temperature to 55 °C promotes the enrichment of hydrogenotrophic methanogens compared to acetoclastic methanogens and other competing bacteria [46, 47]. Profiling the metabolically active community in the samples collected from phases (II) and (III) is necessary for concrete conclusions on hydrogenotrophic methanogens enrichment. Nevertheless, the higher MPR observed in phase (III) (i.e., thermophilic TFBR) may be attributed to the greater abundance of hydrogenotrophic methanogens at this temperature. Although thermophilic anaerobic digestion processes have shown higher process performance, temperatures below 55 °C provide an advantage in terms of BM process stability [48, 49]. Higher temperatures can lead to a more fragile process owing to the lower microbial richness and diversity of catabolism [46]. Comparing phases (II) and (III), no visible changes in the flow structure and stability of the foam along the tube were observed. Achieving a higher MPR in a TFBR system may involve longer biomass enrichment and optimal system design.

Demand-oriented biological methanation in phase (II) In the mesophilic tubular foam bed reactor

The flexibility and stability of the BM process are of paramount importance, considering PtG as an alternative storage technology for surplus renewable electricity [27, 50]. In the scheduled 3-week experiment during phase (II), the mesophilic TFBR was subjected to repeated partial H2 feeding, as shown in Fig. 4a. Previous research has highlighted the advantages of supplying minimal H2 feeding compared to the nominal value, preventing variations in microbial community structure when resources are limited; therefore, a shorter recovery time is needed [27, 50]. A recent microbial study revealed a distinct resource allocation strategy utilized by a methanogenic archaeon under conditions of energy scarcity, diverging fundamentally from the well-studied versatile chemoheterotrophic bacteria like E. coli [51]. This study has shown that methanogens maintain their proteome allocation even at low H2 fluxes, suggesting their capability for rapid recovery [51]. This strategy was also applied in the present study, to avoid either structural or metabolic activity loss during downtime (starvation period).

Fig. 4
figure 4

Time course of various process parameters for the mesophilic tubular foam-bed bioreactor using a partial H2 feeding regime. a Substrate feeding rates; b outlet gas composition; c pH value; d hourly methane production rate (MPR)

In the first week of stable operation, the outlet gas maintained a consistent CH4 content of approximately 93% on weekly average (Fig. 4b). However, upon initiating partial H2 feeding, the amount of non-converted CO2 increased, resulting in a decrease in CH4 content to an average of 30% within 7 days of the middle week (Fig. 4b). The pH slightly fluctuated with H2 feeding changes (average pH = 7.65 ± 0.45), representing the buffering capacity of the liquid phase in capturing the unconverted CO2 during downtime (Fig. 4c). Upon resuming H2 feeding, the conversion of CO2 to CH4 was promptly recommenced and the CH4 content reached its highest value within the 12 h (Fig. 4b). In the third week, with continuous nominal feeding of H2, no process disturbances were detected, indicating resilience against H2 fluctuations experienced in the previous week.

A comparison between the first and second weeks, as depicted in Fig. 4d, reveals that H2 fluctuations contributed to a decline in the hourly MPR and its instability (to demonstrate the variation caused by partial H2 feeding, the MPR is reported here on an hourly basis intentionally). As H2 feeding was reduced by almost half during the second week, the daily MPR also halved; however, in the third week, it regained stability and reached the same level as in the first week. While the H2 conversion yield remained relatively stable, the absolute CO2 conversion yield was reduced by half due to H2 deficiency (Additional file 3, Fig. S.1). Furthermore, the third week demonstrated even more stability in terms of the process results. According to a previous study on the microbial community responses to H2 fluctuations in the BM process, an increase in the abundance of specific methanogens could be possible [27]. Therefore, the BM process in the mesophilic TFBR exhibited robustness against partial H2 feeding and its implementation was expected to be demand-oriented. However, to draw conclusions on the suitability of this system for coupling with the renewable energy sector, more evidence regarding non-linear changes in H2 feeding, aligned with the availability profile and price of the surplus electricity, is needed [50]. Thus far, the BM process systems have demonstrated a unique ability for demand-oriented operation in mild conditions, characterized by controllability and rapid response to changes, distinguishing them from physiochemical processes [13, 52]. Studies on flexibility have indicated that hydrogenotrophic methanogens are generally considered as being resilient and robust against dynamic operation of the BM process [50]. However, literatures have also reported microbial structure or activity changes and their consequential effects on performance during downtime periods [27, 34, 53, 54]. Recovery-time to reach the peak of performance is dependent on several factors, including downtime temperature, duration and feeding gas flow [50]. Optimizing these factors plays a crucial role in the demand-oriented operation of various BM reactor systems.

Perspective and challenges of tubular foam-bed reactor

While previous studies have primarily focussed on preventing foam production in their BM systems [15, 55], the present study uniquely aimed to stabilize micro-bubbles and foam production to enhance the transferability of H2 to the liquid phase. In comparison to the other studies, the laboratory-scale TFBR demonstrated promising and comparable results [6, 13]. Burkhardt et al. highlighted significant differences in reactor performance among various concepts, emphasizing the trade-offs between MPR, CH4 concentration and energy expenditure [13]. They found that while CSTRs can achieve high MPR due to their intense energy input for mixing, this comes at the expense of lower final CH4 concentration and the need for post-modification steps to reach the grid-quality biomethane [13].

The improvement in gaseous substrates availability, higher conversion rates and biomass recycling facilitated the growth of the microbial community. After adding a polymeric surfactant, the MPR in phase (I) improved roughly sevenfold in phase (II) of TFBR, increasing to 13-fold with higher temperature during phase (III). Final gas composition improvements to grid values were also notable in phase (II) and phase (III).

Comparatively, the TFBR achieved a threefold higher MPR than an earlier laboratory-study by Electrochaea in 2013 using a CSTR (9.93 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\)), with the H2 conversion efficiency of about 96% conducted at atmospheric pressure, thermophilic conditions and CO2 and H2 as substrates [15]. Furthermore, in the same study, they improved the CSTR productivity by increasing the pressure (1.2 atm), resulting in an MPR of approximately 47 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\), although with a reduced H2 conversion efficiency of about 80% [15].

In the PtG BioCat project pilot studies by the same group in 2017 using a reactor volume of 3.5 m3, a pressure of 7.8 atm, a temperature of 62 °C and biogas as the feed (35% CO2, 63% CH4), they produced approximately 170 \({\text{m}}_{{\text{CH}}_{4}}^{3}\text{/}{\text{m}}_{\text{R}}^{3}\text{/d}\) of grid-based biomethane [4, 56]. Further investigations could explore the feasibility of high-pressure studies in TFBR within a scaled-up setup, prioritizing process safety. Attention should be given to the recycling of media containing PU-F68 at a larger scale to reduce the costs and address its low biodegradability. Considering the technology readiness levels (TRL), our evaluation places this technology in level 3. This stage, involves testing the TFBR prototype in a laboratory and controlled environment to confirm that it operated as intended. While level 3 signifies an achievement in proving the concept’s feasibility, additional development and testing are typically necessary to advance the technology to higher TRLs.

Exploring the challenges and opportunities of the TFBR, it becomes paramount to delve into the implications of incorporating a surfactant. The investigation should not only encompass the economic and environmental aspects of the surfactant but also should confirm the observed resilience in anaerobic digestion, in general. Furthermore, the dilution of surfactant due to metabolic water production associated with biomethanation should be considered.

Therefore, dedicated studies are warranted to meticulously examine the potential of recycling the liquid phase containing nutrients and PU-F68. Maybe, ultrafiltration could apply to remove water without loosing PU-F68. Concurrently, a vigilant assessment of the long-term impact of the polymeric surfactant on the microbial community is imperative, ensuring the robustness and stability of the biological methanation process. Furthermore, directing additional research efforts towards optimizing gas injection methods to the TFBR can effectively address the pressure drop issue, particularly in large-scale applications. These synergistic endeavors collectively will propel the TFBR’s TRL and underscore its potential as a key player in advancing biomethanation technology within the renewable energy landscape.

Conclusions

In a summary, a distinctive approach was implemented to address the issue of H2 mass transfer to the liquid phase of the BM process by utilizing stabilized liquid foam. This innovative strategy significantly improved the productivity of the tubular system, achieving an output of approximately 30 \({\text{L}}_{{\text{CH}}_{4}}\text{/}{\text{L}}_{\text{R}}\text{/d}\) under thermophilic conditions, while maintaining its grid-base quality. The promising outcome of the partial H2 feeding experiment underscored the flexibility and capacity of the TFBR for dynamic energy conversion. Further studies to support the scale-up of the TFBR are crucial for advancing its potential applications.

Materials and methods

Chemicals and nutrient solutions

The composition of the nutrient solution for microorganism growth is listed in supplementary material, Table S.1. To generate stable liquid foam in the TFBR, a non-ionic polymeric surfactant, Pluronic® F-68 BioChemica (PanReac Applichem, Darmstadt, Germany), was used at a concentration of 1.5% w/v.

Reactor setup and operation conditions

As shown schematically in Fig. 1, the setup primarily consisted of a TR, a liquid recirculation bottle and a polymer electrolyte membrane (PEM) water electrolyzer. CO2, one of the main substrates for the BM process, was supplied from a purchased gas bottle (CO2 4.8, Linde Gas GmbH, Pullach, Germany) while H2, the second main substrate of this process, was generated locally, by splitting water molecules to H2 and O2 using a PEM electrolyzer (E104, Double Electrolyzer, H-TEC Education, College Station, TX, USA).

Tubular bioreactor

In this study, the TR (Fig. 1) consisted of a helix-formed nylon pneumatic air tube (13 m long, 4 mm inner diameter, winding core 100 mm, with connections reaching an approximate working volume of 170 mL, VWR, Germany) placed in a 1L jacketed vessel (Eppendorf AG, Hamburg, Germany) and controlled by two BioFlo®120 systems (Eppendorf, Inc., Enfield, CT, USA). The vessel’s temperature was maintained at 40 °C under mesophilic conditions and 55 °C under thermophilic conditions using a Pt100 probe. Liquid recirculation, substrate feeding, nutrient feeding and biomass harvest were carried out using a pulse-feeding method with the assistance of BioCommand® (Eppendorf, Inc., Enfield, CT, USA) and two peristaltic pumps from the BioFlo®120 systems. Other unused ports of the main vessel and recirculation bottle were sealed with stainless steel plugs or connected to gastight tubing Santoprene® LEZ–SAN, with an internal diameter of 1.6 mm and a thickness of 1.6 mm (Medorex, Nörten-Hardenberg, Germany), which were closed with a luer/lock sampling valve (Eppendorf AG, Hamburg, Germany). The recirculation bottle in Fig. 1 had a volume of 450 mL and the pH of the reactor was controlled in this bottle using ISM® sensors (Inpro 325X (i), Mettler Toledo®, Geissen, Germany).

A total liquid volume of 170 mL, including biomass as BM process biocatalysts, was continuously circulated between the main reactor and the recirculation bottle at a rate of 1.5 mL/min. The liquid level in the recirculation bottle varied based on the feeding rate of gaseous substrates, but stabilized at a fixed level during constant feeding rates. A balance was placed under the liquid recirculation bottle to collect the harvest, which included process water and the supplied nutrient solution.

To achieve high cell density in a short period, the harvest was collected, centrifuged and the biomass was returned to the reactor under anaerobic conditions, as explained in Additional file 1, part S.1. Sampling (12–14 mL) and nutrient feeding were performed through ports on the recirculation bottle.

The gaseous substrates were injected at the tube inlet through an in-line needle injection port. Stabilized bubbles flowed through the tube, as shown in Fig. 1a. The outlet of the tube reached the recirculation bottle, where the processed gas and recirculating liquid were separated. When the headspace of the recirculation bottle reached 80 mbar, the outlet gas was automatically vented, cooled through a gas condenser and further analyzed using a gas analysis system.

Reactor operation

The TR setup was operated in three distinct phases, as presented in Table 1. These extended operational periods included phases dedicated to biomass formation and adaptation to improved substrate feeding. In phase (I), the mesophilic TR was inoculated with biomass obtained from an ongoing BM setup conducted in-house (further information is provided in the Additional file 1: part S.1).

Following approximately 3 months of continuous operation, phase (II) commenced with the introduction of PU-F68 (1.5% w/v) into the liquid phase of the mesophilic reactor, resulting in the transformation of the system into a TFBR (Table 1). Phase (II) spanned over a period of more than 5 months.

Towards the end of this phase, the reactor underwent a week-long challenge involving fluctuating H2 feeding (referred here as a partial H2 feeding experiment). During this experiment, the mesophilic TFBR received nominal H2 feeding (approximately 500 mL/h) for 12 h, followed by a subsequent 12 h period where only 10% of the nominal feeding rate (approximately 50 mL/h) was supplied. In phase (III), the reactor temperature transitioned from mesophilic (40 °C) to thermophilic (55 °C) conditions, as explained in the Additional file 1, part S.1.

Analytics

Gas composition and volume of the outlet gas were continuously monitored using a "GärOnA" system equipped with an integrated gas chromatography (GC) analysis instrument (Gesellschaft zur Förderung von Medizin-, Bio- und Umwelttechnologien e.V. (GMBU), Halle, Germany; mobilGC Elektrochemie Halle GmbH (ECH), Halle, Germany). Further details regarding the specific settings can be found in the reference [27].

The dry weight of biomass was determined using a vacuum filtration unit and Polyethersulfone membrane filters with a pore size of 0.2 μm (Sartorius Stedim Biotech Gmbh, Göttingen, Germany). One mL sample was washed with 13 mL of ultra-pure H2O Milli-Q® in a 15 mL Falcon tube, thoroughly mixed and filtered using pre-dried and weighed membrane filters. These filters were then dried at 70 °C in an oven (Kelvitron® t, Heraeus Instruments, Hanau, Germany) until a stable reading was achieved. The OD600 was measured using a spectrophotometry method (Thermo Fisher Scientific Inc., Madison, WI, USA) and appropriate dilution was applied to obtain readings between 0.0 and 0.9. The OD600 of the undiluted samples was calculated based on the applied dilution factor.

Microscopic images of the foam were captured using a reactor sample and artificial foam generation outside the reactor, through air injection, observed at 100 × and 400 × magnification using a light microscope (Primo Star, Carl Zeiss, Göttingen Germany).

Process parameter estimations

The process performance was assessed by calculating the MPR, relative H2 to CH4 conversion yield \(({\text{Y}}_{\text{rel }}{\text{H}}_{2}\)) and absolute conversion yield of CO2 to CH4 (\({\text{Y}}_{\text{abs}}{{\text{CO}}}_{2}\)). Detailed explanations of these calculations can be found in Additional file 2, of this study, as explained in the literature [27, 57].