Abstract
This research conducts a series of industrial tests on coal reburning of a 600 MW pulverized coal boiler firing lignite, which is one part of a coal reburning demonstration project. When running steadily under 600 MW load, the boiler has an average NO x emission of 274 mg/m3 (O2 content in flue gas is converted to 6%), the NO x emission is reduced by 65.36%. In the meanwhile, loss of ignition (LOI) under coal reburning rarely increases. Three operation conditions — traditional air feeding, air staging and coal reburning — are realized, respectively, during the industrial tests, and the results indicate that coal reburning has the lowest NO x emission, while the traditional air feeding has the highest NO x emission. Under the test conditions, the higher the proportion of the reburning coal, the higher the NO x control can reach.
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This work was presented at the 6th Korea-China Workshop on Clean Energy Technology held at Busan, Korea, July 4–7, 2006.
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Qiu, P., Wu, S., Sun, S. et al. Industrial test on coal re-burning at a 600 MW utility boiler and NO x reduction. Korean J. Chem. Eng. 24, 683–687 (2007). https://doi.org/10.1007/s11814-007-0026-6
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DOI: https://doi.org/10.1007/s11814-007-0026-6