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Increasing the productivity of a pressing-rolling line by combining the operations of upsetting and spreading on the 49-MN press

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Introduction of a technology which involves boring the inside surface of ingot molds has made it possible to reduce the metal consumption coefficient by 20 kg/ton product. The productivity of the pressing-rolling line increased by five wheels after a technology that combines the operations of upsetting and spreading was introduced on a 49-MN press. The line now produces 129 wheels per hour. Stabilization of the weight of the initial semifinished product’ changing of the deformation conditions on the 49-MN press’ and arranging for more regular operation of the pressing-rolling line reduced the number of wheels rejected for scale’ seams’ and defects found by ultrasonic inspection.

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Translated from Metallurg’ No. 4’ pp. 51–54’ April’ 2008.

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Volkov, A.M., Tarasova, V.A., Yandimirov, A.A. et al. Increasing the productivity of a pressing-rolling line by combining the operations of upsetting and spreading on the 49-MN press. Metallurgist 52, 229–234 (2008). https://doi.org/10.1007/s11015-008-9037-8

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  • DOI: https://doi.org/10.1007/s11015-008-9037-8

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