Skip to main content
Log in

Failure Analysis of Nozzle Guide Vane of a Low Pressure Turbine in an Aero Gas Turbine Engine

  • Case History---Peer-Reviewed
  • Published:
Journal of Failure Analysis and Prevention Aims and scope Submit manuscript

Abstract

Failure of low pressure turbine nozzle guide vane (NGV) in an aero gas turbine engine is analyzed to determine its root cause. Forensic and metallurgical investigations are carried out on the NGV failed as well as the failed components of the downstream modules. Failure in the cooling system in the NGV due to crack in the sealing plate was found to be the cause of NGV getting burnt. This failure has caused extensive damages in low pressure turbine modules. Remedial measures are also suggested to prevent such failures.

This is a preview of subscription content, log in via an institution to check access.

Access this article

Price excludes VAT (USA)
Tax calculation will be finalised during checkout.

Instant access to the full article PDF.

Fig. 1
Fig. 2
Fig. 3
Fig. 4
Fig. 5
Fig. 6
Fig. 7
Fig. 8
Fig. 9
Fig. 10
Fig. 11
Fig. 12
Fig. 13
Fig. 14
Fig. 15
Fig. 16

Similar content being viewed by others

References

  1. J. Hour, B.J. Wicks, R.A. Antoniou, An investigation of fatigue failures of turbine blades in a gas turbine engine by mechanical analysis. J. Eng. Fail. Anal. 9(2), 201–211 (2002)

    Article  Google Scholar 

  2. H. Kazempour-Liacy, S. Abouali, M. Akbari-Garakani, Failure analysis of a first stage gas turbine blade. J. Eng. Fail. Anal. 18(1), 517–522 (2011)

    Article  Google Scholar 

  3. S. Suresh, Fatigue of Materials, 2nd edn, (Cambridge University Press, Cambridge, 2003). pp. 256–257

  4. J.A. Bannantine, J.J. Comer, J.L. Handrock, Fundamental of Metal Fatigue Analysis (Prentice Hall Inc, Englewood Cliffs, 1990), pp. 40–87

    Google Scholar 

  5. N. Eliaz, G. Shemesh, R.M. Latanision, Hot corrosion in gas turbine components. J. Eng. Fail. Anal. 9(1), 31–43 (2002)

    Article  Google Scholar 

  6. C.B. Meher-Homji, G. Gabriles, Gas turbine blade failures-causes, avoidance and trouble shooting. Proceedings of 27th Turbomachinery Symposium, 1995

  7. H. Cohen, G.F.C. Rogers, H.I.H. Saravanamuttoo, Gas Turbine Theory, (Wiley, New York, 1996)

  8. Q.P. Zheng, A.K. Jasuja, A.H. Lefebvre, Structure of airblast sprays under high ambient pressure conditions. J. Eng. Gas Turbines Power 119(3), 512–518 (1997)

    Article  Google Scholar 

  9. H.Arthur Lefebvre, GAS Turbine Combustion (CRC Press, Boca Raton, 1998)

    Google Scholar 

Download references

Acknowledgments

The authors are very grateful to the Executive Director, Engine Division, Hindustan Aeronautics Limited, General Manager, Foundry & Forge Division, Hindustan Aeronautics Limited and Chief Executive (Airworthiness), CEMILAC for their kind permission for publishing this paper.

Author information

Authors and Affiliations

Authors

Corresponding author

Correspondence to R. K. Mishra.

Rights and permissions

Reprints and permissions

About this article

Check for updates. Verify currency and authenticity via CrossMark

Cite this article

Mishra, R.K., Thomas, J., Srinivasan, K. et al. Failure Analysis of Nozzle Guide Vane of a Low Pressure Turbine in an Aero Gas Turbine Engine. J Fail. Anal. and Preven. 14, 578–587 (2014). https://doi.org/10.1007/s11668-014-9858-7

Download citation

  • Received:

  • Published:

  • Issue Date:

  • DOI: https://doi.org/10.1007/s11668-014-9858-7

Keywords

Navigation